Update time!

The electronics has arrived!
  • Motor: Topwerpro 2409-12T
  • ESC: Towerpro 18A
  • Battery: 2s1000mAh 25-35C Loong-Max to start with
  • Prop: 8*4 slowfly GWS

21
Hatch cut.

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Break away motor-mount.

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Hinge for the hatch.

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Rare earth magnet for holding the latch.

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One is strong enough to lift the whole plane!

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A servo in place.

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The two other servos in place.

30-2
Pushrod for the tail rudder done.

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I use ball-links from an old T-Rex kit to make my pushrods.

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3mm carbon tube with ball-links

37
Futaba 2.4GHz FASST Receiver mounted.

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Speed-controler in place.

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“Training wheel wings” glued on.

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I used some clear hard plastic to protect the bottom of the spons.

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Out in the snow.

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Testflight!



Initially the plan was just to test-drive it around on the ground because the wife had the car so I couldn’t get to a field.
I walked to the nearest place that I could find with some flat ground and plugged in the battery.

The Hydro handles well on the snow but after a while my fingers got a little to itchy...
I thought that I would take of for just a short bit and land it directly, a little jump with other words.

Well this is how it ended:
43-2
Can you spot it?

44

45-2
Nothing serious, a few minutes of love and glue and she will be in the air again.
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