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Viewing 15 posts - 1 through 15 (of 24 total)
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  • in reply to: Tricopter LR 8000/5200 #62735
    touchthebitum
    Participant

    Yes!!
    Nice temperature and weather after a long bad time with rainy days 😉

    in reply to: Tricopter LR 8000/5200 #62702
    touchthebitum
    Participant

    Tests were made at 1100m above see.
    It was a bit windy.
    Temp was about 25 degrees.
    It ended up with 3% and 9.65v as total remaining voltage.
    Total weight with lipo was under 1kg.

    in reply to: Tricopter LR 8000/5200 #62670
    touchthebitum
    Participant

    Yesterday I tested my 3s 8000mah lipo on my tricopter LR and we are far far away from the hour flightime. I flew with hovering and circle flightpaths and I only got 28.5 min with a 9.65V final voltage.
    I’m very surprised of this result. It was a little windy but I’m very curious to see the results if I made acrobatics flights ….
    Any ideas ?

    in reply to: Betaflight 4.0 #62637
    touchthebitum
    Participant

    Great !
    Thanks Claude !
    I’ll try that.

    in reply to: Betaflight 4.0 #62585
    touchthebitum
    Participant

    Good ( crossed fingers) 😉

    in reply to: Autotune #62579
    touchthebitum
    Participant

    thanks swissfreek 😉

    in reply to: Autotune #62555
    touchthebitum
    Participant

    I kept autotuned values on roll/pitch and kept default values on yaw and it is much better.
    It seems that autotune is not working well on yaw.

    in reply to: Tricopter LR – Firmware (Triflight, iNav)? #62490
    touchthebitum
    Participant

    I have this problem too. I can’t connect Blheli32 suite to my escs. ON Betaflight it is ok, DRonin not.

    in reply to: Tricopter LR 8000/5200 #62469
    touchthebitum
    Participant

    Good!
    If the weather is ok, I’ll test this weekend.

    in reply to: Tricopter LR 8000/5200 #62434
    touchthebitum
    Participant

    I’ll test 😉

    in reply to: Tricopter LR 8000/5200 #62428
    touchthebitum
    Participant

    Thanks 😉 It is far away from the ” over 1 hour ” advertised flightime.
    I’ll post results.

    in reply to: ArduCopter #62391
    touchthebitum
    Participant

    Yesterday I try to keep my copter in hand and test stabilize functions. It doesn’t compensate or it does in an opposite way. I tried to invert servo_1 and servo_2 but nothing changes. It is really weird. All motors turns ok and throttle is ok. HUD commpensation response is ok.
    I can’t connect Blheli32 suite having set up blheli passthrough in full parameter list so I can’t reverse motor rotation direction without desoldering motors wires.
    My tricopter configuration is MOTOR1-CW MOTOR2-CCW MOTOR3-CCW. I wonder if this firmware does support only the all MOTOR-CCW configuration…
    Do you have an idea ?
    Thanks
    Franck

    in reply to: ArduCopter #62362
    touchthebitum
    Participant

    Ok, I’ll try 😉
    It is possible I have it reversed.
    Thanks for your help.
    Franck

    in reply to: ArduCopter #62359
    touchthebitum
    Participant

    When I yaw right with the radio stick , I get 1988 in ch4_in calibration page

    in reply to: ArduCopter #62341
    touchthebitum
    Participant

    Hello
    Thanks for your reply 😉
    What I don’t understand is the normal servo behaviour. I don’t know if it flies …
    When I plug the lipo, the servo goes to the right and turns back to center. Then I arm the copter and all 3 motors work. I take the copter in hand and servo compensates well. Then, I don’t understand the yaw stick response. When I yaw to the right , the servo goes to the right but when I yaw to the left, it remains in the center position. I have the motor 1 (cw) motor 2 (ccw) motor 3 (ccw) configuration.
    Does seem the stick response correct ?
    Thanks
    Franck

Viewing 15 posts - 1 through 15 (of 24 total)